- G38.x was not printing correctly in the $G g-code state reports. Now
fixed.
- When investigating the above issue, it was noticed that G38.x
wouldn’t show at all, but instead a G0 would be printed. This was
unlike the v0.9j master build. It turned out volatile variables do not
like to be defined inside a C struct. These are undefined on how to be
handled. Once pulled out, all weird issues went away.
- Also changed two ‘sizeof()’ statements in the mc_probe() and
probe_state_monitor() functions to be more robust later on.
- Updated the commit logs to individual files for each minor release.
Forgot to update the generating script to account for this.
- G38.x was not printing correctly in the $G g-code state reports. Now
fixed.
- Potential bug regarding volatile variables inside a struct. It has
never been a problem in v0.9, but ran into this during v1.0
development. Just to be safe, the fixes are applied here.
- Updated pre-built firmwares with these two bug fixes.
- G28 and G30’s behavior has been updated from the old NIST g-code
standard to LinuxCNC’s. Previously when an intermediate motion was
programmed, the NIST standard would move all axes to the final G28/30
stored coordinates. LinuxCNC states it only moves the axes specified in
the command.
For example, suppose G28’s stored position is (x,y,z) = (1,2,3) for
simplicity, and we want to do an automated z-axis tool retraction and
then park at the x,y location. `G28 G91 Z5` will first move the Z axis
5mm(or inches) up, then move Z to position 3 in machine coordinates.
Next, the command `G28 G91 X0 Y0` would skip the intermediate move
since distance is zero, but then move only the x and y axes to machine
coordinates 1 and 2, respectively. The z-axis wouldn’t move in this
case, since it wasn’t specified.
This change is intended to make Grbl more LinuxCNC compatible while
making commands, like the shown tool retraction, much easier to
implement.
- Critical fix for M0 program pause. Due to its recent change, it would
cause Grbl to suspend but wouldn’t notify the user of why Grbl was not
doing anything. The state would show IDLE and a cycle start would
resume it. Grbl now enters a HOLD state to better indicate the state
change.
- Critical fix for M2 and M30 program end. As with M0, the state
previously would show IDLE while suspended. Grbl now does not suspend
upon program end and leaves job control to the GUI. Grbl simply reports
a `[Pgm End]` as a feedback message and resets certain g-code modes.
- M2/30 g-code reseting fix. Previously Grbl would soft-reset after an
M2/30, but this was not complaint to the (linuxcnc) g-code standard. It
simply resets [G1,G17,G90,G94,G40,G54,M5,M9,M48] and keeps all other
modes the same.
- M0/M2/M30 check-mode fix. It now does not suspend the machine during
check-mode.
- Minor bug fix related to commands similar to G90.1, but not G90.1,
not reporting an unsupported command.
- Homing cycle refactoring. To help reduce the chance of users
misunderstanding their limit switch wiring, Grbl only moves a short
distance for the locate cycles only. In addition, the homing cycle
pulls-off the limit switch by the pull-off distance to re-engage and
locate home. This should improve its accuracy.
- HOMING_FORCE_ORIGIN now sets the origin to the pull-off location,
rather than where the limit switch was triggered.
- Updated default junction deviation to 0.01mm. Recent tests showed
that this improves Grbl’s cornering behavior a bit.
- Added the ShapeOko3 defaults.
- Added new feedback message `[Pgm End]` for M2/30 notification.
- Limit pin reporting is now a $10 status report option. Requested by
OEMs to help simplify support troubleshooting.
- Apparently inverse time motion were not working for quite some time.
Goes to show how many people actually use it. The calculation was bad
and is now fixed in this update. It should now work correctly.
- `;` comment type is now supported. This is standard on LinuxCNC and
common on 3d printers. It was previously not supported due to not
existing in the NIST standard, which is out-dated.
- New compile-option to ECHO the line received. This should help users
experiencing very weird problems and help diagnose if there is
something amiss in the communication to Grbl.
- New compile-option to use the spindle direction pin D13 as a spindle
enable pin with PWM spindle speed on D11. This feature has been
requested often from the laser cutter community. Since spindle
direction isn’t really of much use, it seemed like good good trade.
Note that M4 spindle enable counter-clock-wise support is removed for
obvious reasons, while M3 and M5 still work.
- Cleaned up the limit pin state reporting option to display only the
state per axis, rather than the whole port. It’s organized by an XYZ
order, 0(low)-1(high), and generally looks like `Lim:001`.
- Separated the control pin state reporting from limit state reporting
as a new compile option. This stayed the same in terms of showing the
entire port in binary, since it’s not anticipated that this will be
used much, if at all.
- Updated some of the gcode source comments regarding supported g-codes.
- G91.1 support added. This g-code sets the arc IJK distance mode to
incremental, which is the default already. This simply helps reduce
parsing errors with certain CAM programs that output this command.
- Max step rate checks weren’t being compiled in if the option was
enabled. Fixed now.
- Alarm codes were not displaying correctly when GUI reporting mode was
enabled. Due to unsigned int problem. Changed codes to positive values
since they aren’t shared with other codes.
- Homing cycle failure reports alarm feedback when the homing cycle is
exited via a reset, interrupted by a safety door switch, or does not
find the limit switch.
- Homing cycle bug fix when not finding the limit switch. It would just
idle before, but now will exit with an alarm.
- Licensing update. Corrected licensing according to lawyer
recommendations. Removed references to other Grbl versions.
- Overhauled the state machine and cleaned up its overall operation.
This involved creating a new ‘suspend’ state for what all external
commands, except real-time commands, are ignored. All hold type states
enter this suspend state.
- Removed ‘auto cycle start’ setting from Grbl. This was not used by
users in its intended way and is somewhat redundant, as GUI manage the
cycle start by streaming. It also muddled up how Grbl should interpret
how and when to execute a g-code block. Removing it made everything
much much simpler.
- Fixed a program pause bug when used with other buffer_sync commands.
- New safety door feature for OEMs. Immediately forces a feed hold and
then de-energizes the machine. Resuming is blocked until the door is
closed. When it is, it re-energizes the system and then resumes on the
normal toolpath.
- Safety door input pin is optional and uses the feed hold pin on A1.
Enabled by config.h define.
- Spindle and coolant re-energizing upon a safety door resume has a
programmable delay time to allow for complete spin up to rpm and
turning on the coolant before resuming motion.
- Safety door-style feed holds can be used instead of regular feed hold
(doesn’t de-energize the machine) with a ‘@‘ character. If the safety
door input pin is not enabled, the system can be resumed at any time.
- Re-organized source code files into a ‘grbl’ directory to lessen one
step in compiling Grbl through the Arduino IDE.
- Added an ‘examples’ directory with an upload .INO sketch to further
simplify compiling and uploading Grbl via the Arduino IDE.
- Updated the Makefile with regard to the source code no longer being
in the root directory. All files generated by compiling is placed in a
separate ‘build’ directory to keep things tidy. The makefile should
operate in the same way as it did before.